罗许国, 钟新谷, 戴公连. 无粘结预应力高性能粉煤灰混凝土桥梁收缩与徐变变形试验研究[J]. 工程力学, 2006, 23(7): 136-141.
引用本文: 罗许国, 钟新谷, 戴公连. 无粘结预应力高性能粉煤灰混凝土桥梁收缩与徐变变形试验研究[J]. 工程力学, 2006, 23(7): 136-141.
LUO Xu-guo, ZHONG Xin-gu, DAI Gong-lian. EXPERIMENTAL STUDY ON THE DEFORMATIONS FOR SHRINKAGE AND CREEP OF BEAMS IN NON-GLUED PRESTRESSED HIGH PERFORMANCE FLY ASH CONCRETE BRIDGES[J]. Engineering Mechanics, 2006, 23(7): 136-141.
Citation: LUO Xu-guo, ZHONG Xin-gu, DAI Gong-lian. EXPERIMENTAL STUDY ON THE DEFORMATIONS FOR SHRINKAGE AND CREEP OF BEAMS IN NON-GLUED PRESTRESSED HIGH PERFORMANCE FLY ASH CONCRETE BRIDGES[J]. Engineering Mechanics, 2006, 23(7): 136-141.

无粘结预应力高性能粉煤灰混凝土桥梁收缩与徐变变形试验研究

EXPERIMENTAL STUDY ON THE DEFORMATIONS FOR SHRINKAGE AND CREEP OF BEAMS IN NON-GLUED PRESTRESSED HIGH PERFORMANCE FLY ASH CONCRETE BRIDGES

  • 摘要: 结合洛湛线的建设,以8根不同掺量的高性能粉煤灰混凝土无粘结预应力桥梁的收缩、徐变试验为基础,研究了不同掺量高性能粉煤灰混凝土在荷载长期作用下收缩、徐变性能及其上拱随时间的变化规律,探讨了温度、湿度等环境因素对不同掺量高性能粉煤灰混凝土收缩、徐变的影响。300多天的实验观测结果表明:高性能粉煤灰掺量20%~40%混凝土梁不但具有良好的工作性能和力学性能,而且长期性能良好,与同强度的未掺高性能粉煤灰的梁相比,其后期强度和抗压弹性模量增大,收缩徐变减小,具有良好的社会和经济效益。

     

    Abstract: Using the construction of the railway between Luoyan and Zhanjiang as background,based upon the experimental results of shrinkage and creep of eight non-glued concrete beams with different mixtures of high-performance fly ash,the shrinkage,creep and camber of beams with different mixtures of high-performance fly ash concrete under long-term loadings are investigated.The effects of the environmental factors such as temperature,humidity are also explored,the experimental results over 300 days indicate that the non-glued concrete beams with 20%~40% high performance fly ash not only have better workability and mechanical properties,but also exhibit better long-term performance.Compared with concrete beams of same strength but without fly ash,they have higher late-stage strength and compressive elastic modulus,lower shrinkage and less creep with desirable social and economic profitability.

     

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